RUBICON EXPL CO inactive
op#732307 // since --// P-5: active
4016 SOUTH BETTER DRIVE, DALLAS
spud_rate
0%
0 of 6 (6mo+)
median_spud_days
--
cancel_rate
0%
0 cancelled
expired_undrilled
6
avg_permits/yr
1
spud_momentum: inactive ⓘBased on wells spudded in the last 6 months compared to the prior 6 months. active_years: 6 horizontal: 0% top_county: SHACKELFORD
window: | type:
permits (30d)
0
vs_prior
0%
counties (30d)
0
avg_depth (30d)
--
hz_pct (30d)
0%
all_time
6
depth_range (30d): -- - -- ft
-- current_portfolio (RRC scheduling system)
total_wells
1
on_schedule
0
producing
0
shut_in
0
acquired
1
from other operators
divested
5
to other operators
counties
SHACKELFORD 1
fields
ROARK (TANNEHILL) 1
cum_oil: 4,321 BBL cum_gas: 0 MCF
-- wells_operated (1)
| API | LEASE | FIELD | COUNTY | STATUS | SCHED |
|---|---|---|---|---|---|
| 42-417-36434 | NAIL 135 | ROARK (TANNEHILL) | SHACKELFORD | — | N |
-- production_history
-- permit_history (all operated wells — latest 15)
view all >>| SOURCE | PERMIT | API | TYPE | LEASE | COUNTY | ISSUED | FROM/TO |
|---|---|---|---|---|---|---|---|
| divested | 358142 | 42-417-37263 | DRILL | NAIL 150 E-1 | SHACKELFORD | 1989-04-20 | to: FTC CONSULTING LLC |
| divested | 350052 | 42-417-37194 | DRILL | NAIL 150F | SHACKELFORD | 1988-08-12 | to: ROBICAN EXPLORATION CO. |
| divested | 348718 | 42-417-37186 | DRILL | NAIL 150F | SHACKELFORD | 1988-07-13 | to: RUBICON EXPLORATION COMPANY |
| divested | 337692 | 42-417-37114 | DRILL | NAIL 150E | SHACKELFORD | 1987-10-21 | to: FTC CONSULTING LLC |
| divested | 325268 | 42-367-33027 | DRILL | FLOYD, JAMES W. | PARKER | 1987-01-13 | to: RUBICON EXPLORATION COMPANY |
| acquired | 280985 | 42-417-36434 | DRILL | NAIL "135" | SHACKELFORD | 1985-07-24 | from: MIDWOOD PETROLEUM INC. |
-- permit_activity
[ no data ]