42-367-31108

Final Completion

CLARK UNIT

PARKER County · District 7 · MKS CONSULTING CORPORATION · CABBAGE PATCH (BIG SALINE)

RRC Lookup

Permits

2

Max Depth

5,685 ft

First Permit

1978-04-27

Latest Activity

1994-04-13

Lifespan

16 yrs

Regulatory Status

Schedule

OFF SCHEDULE

Completion

1978-07-20

Shut-In

Plugged

!

EWA / Production operator mismatch

Scheduling: MKS CONSULTING CORPORATION ≠ Production: SOMERSET OPERATING, LLC (reported 2025-10)

!

EWA / Permit operator mismatch

Scheduling: MKS CONSULTING CORPORATION ≠ Permit: DYNAMIC PRODUCTION, INC.

Resolved via: schedulingMKS CONSULTING CORPORATION

Production Summary

Cum Oil

bbl

Cum Gas

mcf

First Production

1993-01

Last Production

2026-03

Lease Production

Production is reported at the lease level. View production data, decline curves, and history on the lease page.

Permit Applications (2)

#422872 A DYNAMIC PRODUCTION, INC.
received 1994-04-11
#22982 A RAW ENERGY CORPORATION
received 1978-04-27

Well Details

Well Number
1
Max Depth
5,685 ft
Drill Type
Vertical
County
PARKER
District
7
Completed
1978-07-20

Operator

Location
WEATHERFORD
P-5 Status
Y (filed 2005-06-10)
Cum Oil (all leases)
6,944 bbl
Cum Gas (all leases)
7,666,510 mcf
Total Permits
6

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